Results 131 to 140 of 156
Thread: Rumba and Auto-Bed level
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05-03-2015, 03:35 PM #131
- Join Date
- Feb 2015
- Location
- Miami
- Posts
- 12
I came here just to tell you I have no idea why the m280 command doesnt work once the deactivate_servo is enabled. I searched for it and found nothing but I didnt really look too hard since I just use the m280 command to get my servo positions and go back in and enable the deacivate_servo_delay. This occurred with both makerfarm's marlin firmware and dacb's.
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05-03-2015, 05:47 PM #132
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05-03-2015, 06:08 PM #133
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05-04-2015, 12:17 AM #134
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05-04-2015, 04:32 AM #135OK, sorry to be dense... I'm pretty sure you are not saying this. But the 'M280 command...' was not part of the #define. Right?
Assuming this is true... Something very strange is going on...
#define PROBE_SERVO_DEACTIVATION_DELAY 300
then the M280 command does nothing
when the entry in config.h is:
//#define PROBE_SERVO_DEACTIVATION_DELAY 300
then the M280 command works as expected.
Sorry for the poor wording.
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05-04-2015, 11:42 AM #136
Could this be why?
The firmware I am using is the one pointed i3v 12" build notes:
Marlin_RUMBA_i3v_GLCDPercent at https://drive.google.com/file/d/0B80...BCdkdUaDg/view
Reading through numerous threads it appears that Marlin_Marlin_v1 at https://github.com/beckdac/Marlin
is more up to date and is the better way to go. If that is the case I'll start playing around with that version and see what happens.
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05-04-2015, 12:06 PM #137
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05-08-2015, 09:38 PM #138
Resolved!
OK, spent the last few days playing with software and Raspberry Pi's!
I now have the BeckDac version running, and the M280 command works as advertised regardless of whether #define PROBE_SERVO_DEACTIVATION_DELAY 300 is active or not.
To get the version running required 1 change to the pins.h file and about a dozen changes to the config.h file. All is running pretty well now, and the ABL is behaving.
If any one wants to know the changes I made, let me know.
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05-17-2015, 07:24 PM #139
- Join Date
- Feb 2015
- Posts
- 371
Urrg!
I am at my wits end. I cannot get my first layer to stick anymore. I cleaned out the nozzle and had to reset my offsets. Followed the same procedure as before but my first layer is not sticking. I measured and remeasured everything. When I run a G29 command and pause the print in the first layer it measures fine. The machine reads .2 and the feelers confirm this. Trouble is my prints don't stick.
I was advised to increase the offset in the firmware to bring the nozzle closer but this doesn't make sense to me. Should the measurements match? If the machine thinks it is at .2 the actual nozzle should be at .2. This just makes sense to me.
What am I missing in the slicer to get this to stick?
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05-26-2015, 02:00 PM #140
- Join Date
- Feb 2015
- Location
- Flagstaff, AZ
- Posts
- 73
Hi All I have purchased the micro switch and servo that is referenced in the zenmaster videos and will be printing Clough42's cooling shroud and ABL parts soon. I quickly read through all 14 pages of this post and was overwhelmed.
After I install the parts would the proper course of events be as follows?
1. Update my firmware from the default that I got from Makerfarm to the newest version?
2. Follow steps in post number 118 on this thread by ex-egll.
that it?
New member with print issue
06-11-2024, 08:57 AM in Tips, Tricks and Tech Help