Issue is solved. It turned out to be a problem in EEPROM settings. I sent an M502 and then M500 and the issue disappeared. I had loaded default firmware from the LCD control panel several times...
Type: Posts; User: Drone
Issue is solved. It turned out to be a problem in EEPROM settings. I sent an M502 and then M500 and the issue disappeared. I had loaded default firmware from the LCD control panel several times...
Just tried it with the DACB fork and the same issue exists. Also tried changing the Z offset at 2.8mm instead of the measured 1.8mm offset that I need with my servo and it made no difference, it was...
I know it's something I have done, nothing new there...lol. I just downloaded the DACB fork and am doing a compare now to get my settings transferred and I will give that a try. I would have wound up...
Thanks for the help Abu, it's really appreciated.
After G28 in Pronterface shows 2.86mm with a measured (manual controls used in Pronterface to desired print height of tight with a sheet of paper)...
Yes I do. Z_RAISE_BEFORE_HOMING 4, Z_RAISE_BEFORE_PROBING 4, Z_RAISE_BETWEEN_PROBINGS 2. And all those settings work, although only the Z_RAISE_BEFORE_HOMING might apply since the offset occurs just...
When using ABL I have a Z offset that I haven't been able to sort and could use some advice. When I issue a G28 the X and Y both show 0 with an M114 after the homing command, but the Z shows 2.86. My...